Archive for July, 2012

Dean’s custom amplifier build progress

July 17, 2012

Here is the 2nd in our occasional series of blogs where we publish a visual progress report of a custom-order amp build. This example shows a Blue Mood series amp chassis under way for Dean Gardiner. This amp is a customised variation on the Blue Mood concept, with the addition of a fully-featured valve (tube) driven FX Loop.

The FX Loop features separate Send & Return level controls, as well as separate Send & Return buffer stages. Obviously the Return buffer stage can be configured as an additional gain stage, or purely just to balance the wet signal against the dry signal. The FX Loop can be activated or bypassed by means of a toggle switch mounted on the front control panel. There is no need to be messing around at the rear of the amp in the middle of a gig or session.

This 18 watt Blue Mood head is built around a pair of 6V6 output valves, with power transformer from the very fine Harbuch company of Sydney, plus output transformer & choke from the very fine Mercury Magnetics company (USA). The 6V6’s can be operated in fixed-bias mode for maximum power & dynamic range, or cathode-bias mode for a sweeter tone & more compression (activated rear panel).

Rectification of the high voltage supply on this model is handled by a GZ34/5AR4 rectifier valve (tube). The basic tonality of the Blue Mood amp is inspired by everyone’s favourite early 1960’s amp from California, as exemplified by the Mark Knopflers, the Stevie Ray’s & the Brian Setzer’s of the guitar world. We just go out of our way to make it a little fatter, a little warmer & a little sweeter.

The front panel controls are as follows: single high-impedance input jack, volume, treble, middle, bass (with EQ pull-shift), FX Loop send level & send jack, FX Loop activate/bypass switch, FX Loop return jack & return level, (active) prescence control, master volume (pull activate), standby switch, power on/off switch, neon power on indicator.

The rear panel controls are as follows: 240V/IEC power inlet; mains fuse, HV (high voltage supply) fuse; bold/vintage switch (selects mode of operation for 6V6’s), bias test points (for 6V6’s), line/DI jack, pair of speaker jacks (wired in parallel), speaker impedance selector switch.

The Richards Amplifier Company – Australia. Each & every amplifier is individually hand-assembled, hand-wired, one at a time, by one person from beginning to end, to a specific customer order.

A Modification to the Laney LC30-II

July 10, 2012

A new customer for us, Peter Timperley, delivered his Laney LC30 II 1×12 combo to the workshop for a general service, but with a special request. Peter wanted to restore the sweet tone that previously existed with this amp, but also wanted to know if we could install a full power/half power switch. The obvious way to implement this mod would be to switch out one pair of the quartet of EL84 power output valves, and correct the impedance mismatch that this introduces by utilising the impedance selector switch on the rear panel.

In other words, we need to increase the primary impedance that the EL84’s require from 4000 ohms a-a (anode to anode) for a quartet, to 8000 ohms a-a for a pair. We can achieve that by driving the internal 8 ohm speaker from the 4 ohm connection to the output transformer (see photo #5). That is not the full story, however, as this amp employs a cathode-bias configuration for the EL84’s, so when we switch to half-power we also need to change the bias circuitry appropriately, otherwise the EL84’s will be quite seriously under-biased, resulting in certain destruction.

There is not much depth from the rear of the cab to the rear panel of the amp chassis, so we selected a low profile DPST (double-pole, single-throw) rocker switch to mount on the rear panel. One pole is used to switch out (in this case) the outer pair of EL84’s in low-power mode, leaving the inner pair activated for both scenarios. The second pole is used to switch in an additional cathode-bias resistor (plus cathode bypass capacitor) in series with the existing p.c.b. mounted bias components. By this method, the bias voltage is maintained exactly the same, regardless of mode of operation.

Creating a 19 x 22mm hole for the rocker switch on the rear of the chassis really isn’t much fun at all, unless you happen to own a hydraulic hole punch. The cathode pins (pin 3) on the EL84 9-pin sockets were rewired, with the inner & outer pairs now having separate paths to the switch. You can see from the photos, the additional cathode-bias components are wired on a small tagstrip installed conveniently near the valve sockets. One end of these components will be wired back to the original cathode bias resistor, on the main board, and from there to ground (earth).

We added some Dymo labelling on the rear panel to finish the job. How successful was the mod ? The final power output test resulted in 32 watts/8 ohms full-power, and 17 watts/8 ohms half-power. The tonal quality in half-power mode was in no way inferior to full-power, in fact it might have been a tad sweeter ! Peter contacted us after taking the amp home to confirm he was very pleased with the result. As part of a general service, prior to implementing the mod request, we replaced corroded input & output jacks, cleaned all pots with FaderLube, replaced a dodgy Standby switch, and replaced some high voltage electrolytic capacitors with selected upgraded caps. IR.

Vaughan’s JCM2000 TSL100 major repair

July 1, 2012

Vaughan B. is a loyal regular customer on the NSW Central Coast since way back when he was using a Rocktron rig. In more recent times he updated to a Marshall JCM2000 TSL100 head, which we also have been servicing for him. A couple of months ago the amp “just stopped” for no apparent reason, so back to the workshop it came.

We already had a few TSL100’s in the workshop with similar symptoms, so we had a pretty good idea what might be wrong. Preliminary examination of Vaughan’s amp revealed that the 2 amp slow-blow mains fuse was blown and one pair of the existing EL34 output valves had experienced some kind of melt-down. In other words they had begun to draw more & more current, increasing out of control until finally the fuse blew.

Unfortunately, the fuse didn’t blow quickly enough to save the amp from further (expensive) damage, as further testing revealed that the primary winding of the Dagnall power transformer had gone S/C (short-circuit). So far we will have to replace the quad of EL34 output valves, plus the power transformer. What could have caused such a scenario ? From past experiences with this specific model we have learned (the hard way) that some of the main boards have left the factory with inappropriate components loaded, and/or some boards have developed leakage paths which significantly upset the normal DC voltage conditions.

Before you all start panicking, this scenario does not apply to every single TSL100, just some of them, and they are likely to have been manufactured earlier in the life cycle of this model, rather than later. Looking at the photo to the right, you can see that the main board is the one that all the valves (tubes) plug into, ie the valve sockets are p.c.b. mounted. Most of the valve circuitry is mounted on the board, in particular all of the phase-inverter and power amp valve circuitry.

The problem with Vaughan’s board is that a leakage path developed between the high voltage tracks & pads and the bias supply to one pair of EL34’s in particular. We have previously proven this to be true by powering up a faulty amp with the EL34’s removed, and a DVM (digital voltmeter) connected between pin 5 of one of the EL34 sockets & earth (ground). Over a period of time it was easy to observe the bias voltage to one pair of the EL34 sockets gradually drop quite significantly. This would result in a runaway condition for that pair of valves, just drawing more & more current.

You can see from the photo to the right that components/tracks/pads are packed tightly together in this design, regardless of the design rules concerning high voltage on p.c.b.’s. Nevertheless, in the numerous TSL100 amps where we have replaced the main board altogether, the repair has been successful, so the latest issue of this board appears to have had the problem corrected. But – back to Vaughan’s amp: we therefore ordered in a new power transformer, a new main board, and a matched quad of the very nice Mullard (reissue) EL34’s from New Sensor.

To sum up, we replaced the transformer, board & output valves in that order, with a successful rebias of the EL34’s and conducted the usual power output tests (30V/8 ohms = 110 watts), burn-in tests & electrical safety test. The final cost of this major repair was significant – almost the resale value of this amp in the current economic climate, but at least Vaughan now has a reliable TSL100 to gig with. Vaughan B. is a very decent guy, and was happy to pay the estimated cost of repairs in full prior to commencement, so that we wouldn’t be out of pocket. We truly appreciate that !